Voices From The Garage


Winter! Finally here and time to gather my resources

With the REAL cold weather, as opposed to the not so bad weather we had up to now, it is time to organize for the work that needs to be done in the spring. Time for all the indoor stuff. The hard part right now is getting motivated.What I feel like doing is just hibernate. Or play some Gears of War and veg out. Not any real work.

I actually have lots of stuff to do. Since I have the 70 back with solid floor pans I can put it back together so I can  cruise it around this season.  And now that the dash is completed for the 54 I can replant that in the car.  Then I can follow it up with the wiring system. And I may even get around to redoing the roof paint on the 65 but dunno yet. Got the trim pieces just need to orchestrate the paint.

There may even be a PT Cruiser project in the making! Stay tuned!

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Warm weather means progress. Sorta Maybe Kinda
70 Mustang Coupe

70 Mustang coupe

Squeaky Toy is back home. Actually it has been here since Dec 27. Today was productive and the 50ish weather was awesome! I did get the dash and brace back in. No problem. Put the seats back in … Problem! When I sat down in the driver seat something didn’t look quite right. So a bit of surveying the area revealed that apparently the new repop seat riser is not the same height as the factory Ford unit. Crap! A quick run to the house and flipping through the catalog revealed that I did have the correct piece installed. I have run into this in the past and it is not that uncommon  Kinda like an inch shorter all the way around. No biggie, now that I know what the logistics are! A set of one inch risers on the driver seat slide rails will solve the problem easily. So it’s off to my steel guy to get some square tubing. Another project for another day.

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The new face for the 54
October 26, 2010, 11:48 am
Filed under: 54 Ford Lowrider, General, In the shop, Maybe next week, Projects

Well here are the pics of all the major pieces parts for the face of the54 motor. All painted and fresh. Now I get to put it all together and finish off the reassembly of the front face of the engine.

Things to do on another day! Have to make the trip out to NPD for the bolt kit and some other stuff. Later this week maybe.

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Some 54 engine work in progress
October 14, 2010, 5:45 pm
Filed under: 54 Ford Lowrider, In the shop, Maybe next week, Projects

Part 1 – Retro Water Pump

Replacing the water pump on this project was actually an option on my part. Didn’t really have to but I decided to refit the motor. It has to do with which side the lower water outlet is on so that it matches the radiator. We are currently using a 65 Mustang radiator. It also gets tangled up with the Serpentine belt vs V-belt pump drive direction issues.

The simple solution was to back date to a 65 Mustang pump setup. Pulleys, pump and cover. Cheap, v-belt drive and the right outlet for the 65 Mustang radiator we are using. Now with that decided upon there is another front timing cover related issue I had to deal with. Why the cover you ask? Because of the fuel pump stuff! That’s why!!

Part 2 – Retro Fuel Pump

fuel pump

F100 fuel pump with integrated filter housing

The fuel pump decision was actually very simple. No electric fuel pumps allowed! I am going to use is a 70 Ford F100 mechanical fuel pump. I chose this particular one because it is easy to get and the plus is that it has the fuel filter canister built into the pump housing. One less thing to locate and plumb. The intake configuration is such that I will keep the cast iron intake and transplant a two barrel Holley R-4778 onto it. Now we get to the reason for the timing cover dance. The motor is of 86 vintage. Which by nature is a fuel injected car. While the front cover has the fuel pump mount pad, it is not machined through. Also because it came out of a fuel injected donor car the timing drive does not have the cam eccentric needed to actuate the mechanical fuel pump. Not an earthshaking issue but it will involve some mixing and matching to get the right cover / pump drive combo. Got some extras in the shop so we should be able to figure it out.

Front cover off

Open front timing area

After a bit of sweat equity and brute force applied sparingly I was able to get the crankshaft bolt to release. I did have to fab a bracket to stop the crankshaft from turning while I applied a 24 inch long 3/4 inch drive breaker bar and 24 inch extension to it. Air tools were initially considered as an option but, after some technical consultation with Mr. Campbell (aka Captain Crankshaft) we were concerned for breaking the bolt and/or the crank nose so I opted for manual labor. It finally did come loose. It appears that someone in the past had grossly overtightened that bad boy down to the point that it severely dished the thick washer under it! The harmonic balancer came off uneventfully. With it off I was able to remove the timing cover and to my amazement there was an eccentric already in place. A quick inspection did show some slop in the timing chain which did have the nylon shelled gear set. So a replacement with an all steel set is ln order. A swap out for an earlier cover gets a fuel pump access and a dipstick hole.

Now all that is left to be done is detail the cover and paint it. A new timing chain set and cover gasket set will seal it all back up. The 70 Ford F100 fuel pump is an easy get. So for now we are at a pause to get parts gathered.

Well another mystery solved and another segment of the project done…for now. Intake needs to be be blasted and painted. Working on it!!!! Chill out!

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Face off! of the 70 Mustang motor
May 29, 2010, 8:55 pm
Filed under: 70 Mustang Coupe, General, In the shop, Maybe next week, Projects

70 Mustang Coupe

70 Mustang Coupe

I finally got to the removal of the front timing cover of the 70 motor. After getting all the other goofy stuff out of the way I was finally able to remove the front timing cover in order to find out why something up front was growling and also why we were slinging oil out the crank. It was a discovery that the water pump was an original D0 unit and the bearings had finally expired causing the growling. As for the leaking oil that became obvious when I removed the cover. The crank seal was age cracked in 4 places and was also original in very poor condition. The cover showed signs of being removed at some point before I got it because the goofies used red RTV to seal it back, They did cut away the front section of the pan seals but just red RTV’d it all back together.

Now with the factory front cover, crank seal and water pump still installed we are confused as to why this cover was removed at all. There is some play in the timing chain so it will be replaced before we reassemble the front area. So we will get the cover cleaned and painted, the new water pump is already painted and the new gasket set is here too. So as soon as I can prep and paint the factory cover and get a new chain we, er….. I, will put it all back together. A project for another day!

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